Thursday, December 11, 2008

Saturday 12/6/08

Attendance: Kevin Burns, Terry Adolphson

Kevin: We worked on demoing the robot for the FLL teams; we also got wired and programmed the arm. We found that the mounting of the second arm motor caused the arm to start clicking and fall. The robot was able to climb the ramp and hold it down on its own. We found some problems in the arm in that it can hit sensitive parts of the robot and can get shoved under the robot.s

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